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Thread: Threedogs motor thread

  1. #201
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    Good to hear it's about to all b fixed for ya TD! Well done to Mark and Jaysee.
    Some unusually high temps next 2-3 days for April. So that should test the system a bit once it's all together.
    2005 TD42TI

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  3. #202
    Patrol God threedogs's Avatar
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    Yeah all togaether a huge thanks to all invovled, now after going for spin around the block
    my heater hoses have turned up their toes, will be a quick fix once its cooled,, as it looks like
    the OE clamps have cut the oe hose>
    I have enough hose to cut it and re do it properly, Going to buy a ship load of worm
    drive clamps and remove all OE clamps
    Again a big thanks to John and Mark and all the others
    04 ST 3lt auto, not enough Mods to keep me happy, but getting there

  4. #203
    Legendary jay see's Avatar
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    Just as I was leaving, I mentioned to John that this may be why his engine temps take a long time to get to operating temperature, it's losing pressure. He did point out that this is the same spot where it was pouring out the other day, right above the dump pipe this will explains all the steam.

    Again I had to leave it unfinished. In bed now just about to go sleepies.

    Best to pull off both heater hoses at both ends to check, but it's definitely one. As you touch it it's squirting.

    Keep us informed John.
    12/97 GEE YOU
    4.5lt Gas blower. Lots of mods to come.....all in good time.

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    threedogs (18th April 2016)

  6. #204
    Patrol God threedogs's Avatar
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    Cut the last 50mm off just to get me mobile, Thats the first time I've
    had a problem with the heater hose so maybe the new radiator made this surface.
    Anyway it was a 5 min fix. I'm already onto Mark about replacements

    EDIT since Ive owned it the temp has been very slow to rise.
    OE gauge shows its at temp after 4k, now the ecu-talk would
    show 62 degrees at the same time.
    Attached Images Attached Images
    Last edited by threedogs; 18th April 2016 at 02:33 PM.
    04 ST 3lt auto, not enough Mods to keep me happy, but getting there

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    BigRAWesty (18th April 2016)

  8. #205
    Patrol God threedogs's Avatar
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    Having a heap of Hi-density foam I sliced some and forced it between the
    radiator and the rad support panel along the top doing the sides will be
    trickier But Ill get there. one less job lol
    04 ST 3lt auto, not enough Mods to keep me happy, but getting there

  9. #206
    Patrol God taslucas's Avatar
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    So what was the actual original problem?
    A leaking thermostat housing?

    >>>tappin from tassie
    Hello from Under Down Under!

  10. #207
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    Quote Originally Posted by taslucas View Post
    So what was the actual original problem?
    A leaking thermostat housing?

    >>>tappin from tassie
    I think it was the radiator... But i'm curious to see whether it was that. With everything plugged up now and still overheats well then ...

    Also now your cars back on the road John, will see you at Roofys party !!!!??
    2005 TD42TI

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    Sir Roofy (18th April 2016), threedogs (19th April 2016)

  12. #208
    Legendary jay see's Avatar
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    Quote Originally Posted by taslucas View Post
    So what was the actual original problem?
    A leaking thermostat housing?

    >>>tappin from tassie
    Not think so, the bolts were pretty tight even coming out, that's what I think stuffed the thread.

    John did test both thermostats and both worked, and the radiator didn't look all that good, so I reckon Hodge might be right.
    New radiator, new cap, new thermostat, clutch fan good resistance, water pump no leaks, so if there's a problem now it's the tiniest of things or its internal.

    Have you gone for a spin yet John?
    Please tell me that's its good.
    Last edited by jay see; 18th April 2016 at 05:17 PM.
    12/97 GEE YOU
    4.5lt Gas blower. Lots of mods to come.....all in good time.

  13. #209
    Patrol God threedogs's Avatar
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    ROAD REPORT::::::: went to my surgeons this morning about 35K in morning traffic. {Opposite RMH}
    played up all the way but stop start traffic helped keep temps stable.
    The drive home was a different matter it just got hotter and hotter, so pulled
    over near Bunnings on Ballarat road for those that know, Let it cool a touch
    and filled up with water, up the road same thing happen, Im really really happy
    at this stage. lol So I decided to swap the rad fan relay for the aircon, doing this
    enabled me to drive normally on the way home with temps staying even and
    even recovering on the last 5 k of my trip. Me thinks that rad fan has not been working
    But happy now I can drive it through the gears, without it overheating

    Re Roofys Party Ive booked a seat with Mego, but all depends how Im feeling.
    AH just to sit in those seats oooooohoooooohoo
    Last edited by threedogs; 19th April 2016 at 12:01 PM.
    04 ST 3lt auto, not enough Mods to keep me happy, but getting there

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    BigRAWesty (19th April 2016), mudnut (19th April 2016)

  15. #210
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    I'm unsure whether I should say " good to hear" because as far as I can understand your message it's still overheating ???

    Sent from my SM-G920I using Tapatalk
    2005 TD42TI

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