OUR VIDEOS GALLERY MEMBER SPONSORSHIP VENDOR SPONSORSHIP

User Tag List

Page 2 of 3 FirstFirst 123 LastLast
Results 11 to 20 of 22

Thread: zd30 common rail severe lose of power very hard to start

  1. #11
    Legendary happygu's Avatar
    Join Date
    Aug 2012
    Location
    Melbourne
    Posts
    3,019
    Thanks
    122
    Thanked 1,037 Times in 846 Posts
    Mentioned
    2 Post(s)
    Tagged
    0 Thread(s)
    Have you checked the fuel lines for any moist spots, which would indicate a split or air leak?


    Have you checked the fuel filter is sealing properly?


    It sounds like you may have air in the fuel line, although then it might not run at all .... very perplexing

    Mic
    Last edited by happygu; 12th March 2014 at 06:28 PM.
    GU PATROL 2011 Ti, with goodies...

  2. #12
    Beginner
    Join Date
    Mar 2014
    Posts
    11
    Thanks
    9
    Thanked 0 Times in 0 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    I have checked the relief valve and that is passing, trying too check current from prrssure sensor to ecu, i dont have a complete circuit there cozmy dp chip isnt lighting up, i have plenty of fuel comming back threw the return line so the pump is ruled out, doing my head in, will be for sale as soon as its running

  3. #13
    Advanced patrolman123's Avatar
    Join Date
    Mar 2014
    Location
    melb vic
    Posts
    41
    Thanks
    16
    Thanked 17 Times in 8 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    if u havent fixed it yet try dissconecting fuel pressure reg and try start it and see how that goes. dont drive it though. doing this will give rail full fuel and eliminate any pressure probs with rail or injectors. will sound very noisy but dont stress its normal when u do this

  4. The Following User Says Thank You to patrolman123 For This Useful Post:

    pootrol07 (20th March 2014)

  5. #14
    Beginner
    Join Date
    Mar 2014
    Posts
    11
    Thanks
    9
    Thanked 0 Times in 0 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Just replaced the whole rail....and still not winning. Sending the ecu off for testing as I have current going up the negative wire to the fps. Very costly exercise! Not a happy patrol owner

  6. #15
    Advanced patrolman123's Avatar
    Join Date
    Mar 2014
    Location
    melb vic
    Posts
    41
    Thanks
    16
    Thanked 17 Times in 8 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Have u checked for shorts? ? Where did u test that current from in the loom? Try checking it at ecu. If your any good with wiring try removing pin from ecu connector and test straight outta the ecu.
    pootrol with the lot! :

  7. #16
    Advanced patrolman123's Avatar
    Join Date
    Mar 2014
    Location
    melb vic
    Posts
    41
    Thanks
    16
    Thanked 17 Times in 8 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Also try disconnecting the dp chip and put it back to factory to eliminate a problem with the chip
    pootrol with the lot! :

  8. #17
    Legendary happygu's Avatar
    Join Date
    Aug 2012
    Location
    Melbourne
    Posts
    3,019
    Thanks
    122
    Thanked 1,037 Times in 846 Posts
    Mentioned
    2 Post(s)
    Tagged
    0 Thread(s)
    Quote Originally Posted by pootrol07 View Post
    I have checked the relief valve and that is passing, trying too check current from prrssure sensor to ecu, i dont have a complete circuit there cozmy dp chip isnt lighting up, i have plenty of fuel comming back threw the return line so the pump is ruled out, doing my head in, will be for sale as soon as its running
    I would be looking for the problem where the DP Chip doesn't have power, or doesn't have the LED on .....
    GU PATROL 2011 Ti, with goodies...

  9. #18
    Beginner
    Join Date
    Mar 2014
    Posts
    11
    Thanks
    9
    Thanked 0 Times in 0 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    Sent the ecu off to get checked, ended up being fried.
    Got a new ecu and programed the key ect, not have fault code p1625 which means i have to recalibrate the injectors to the ecu. Will be doing this tonite

  10. #19
    Patrol God threedogs's Avatar
    Join Date
    Jun 2012
    Location
    Melb
    Posts
    31,635
    Thanks
    10,350
    Thanked 9,963 Times in 7,394 Posts
    Mentioned
    113 Post(s)
    Tagged
    2 Thread(s)
    that's sounds good, did they say how it got "fried"
    So you're keeping it now ???
    04 ST 3lt auto, not enough Mods to keep me happy, but getting there

  11. #20
    Beginner
    Join Date
    Mar 2014
    Posts
    11
    Thanks
    9
    Thanked 0 Times in 0 Posts
    Mentioned
    0 Post(s)
    Tagged
    0 Thread(s)
    They suspect the dp chip sent power down the earth wire which took out the earth on the ecu on the pressure sense side of things but they said they couldn't be 100% sure. Sent it to injectronics in Melbourne.
    I couldn't get the injecterz calibrated as they scan tool i was using isnt up to date so i have to now take it to nissan.
    Gonna keep it now as it owes me $4500 in the last 6 weeks

Page 2 of 3 FirstFirst 123 LastLast

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •