What were all your gauges showing when this happened? It doesn't sound good but the white smoke could have been steam and it may just be a cracked head.
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What were all your gauges showing when this happened? It doesn't sound good but the white smoke could have been steam and it may just be a cracked head.
ok great, i can answer all that.
boost was around the 18-20psi mark, EGT @ around 470degc
most of the smoke from the engine bay came from the hose at the bottom of the catch can blowing off (due to the catch can filling up with oil) and blowing oil all over the side of the motor. there was a real burned smell in the bay when i was finally ina safe place to pop the hood. the motor still runs, but its super super rough and white smoke comes out of the exhaust. i didnt see if the radiator was down on water but i know that the motor lost a ship load of oil it went from full to below empty when the NRMA mech tried to start it to do his initial diagnosis.
ok im not fussed mate, obviously i will be more dissapointed, but regardless the bloody thing has to be fixed. thanks for the advice though, its really appreciated. when i know more ill be posting it up on here. question though, the EGTs were that hot from what i believe? the rings/pistons wouldnt be likely to melt at those temps would they? especially considering i was on the road for not even 5 mins so the motor hadnt been workign that hard prior to it going kaput?
btw i have to drive home now and broke my smart phone on monday(im have a great luck streak of late) ill check this thread later tonight, sorry if i cant answer any questions till then.
That sucks Nic, here's hoping it's a repair on the easier side. Is the valve still in one piece, just blocked or stuck open, or are there bits missing?
Far out Nico, you're a calm little cookie mate. If that was me i would be farking killing people....just sayin
Let me know if you need anything mate but nothing out of my engine,thank you!...LOL