22nd January 2014, 09:47 AM
Any chance that theres nothing sucked into
the fuel line
the way ive read it sounds like air a bit like seals drying out
in the pump or filter it is your daily or does it sit around till the...
22nd January 2014, 09:41 AM
Why not replace all fuel line and return lines,
cost wouldn't be huge IMO
Then you can tick that box, one less thing
22nd January 2014, 09:09 AM
The relay swap made a marked improvement for nearly 4 months did you have any stoppages in that time?
20th January 2014, 11:02 PM
DTC 707 can be set by a blocked fuel filter or air being sucked in the fuel lines.
20th January 2014, 09:56 PM
A quick check run engine and move the relay side to side a few times if engine stalls spray and work in and out then try again, cant hurt and no cost.
20th January 2014, 09:08 PM
I'd be finding out whar fault 77 is... Unless you know.
13th October 2013, 06:17 PM
Thanks for the update. Has your A/C stopped working at any stage or doesn't seem as cold as before the relay swap?.
Please note, the relay swap will not affect the interior fan operation.
It...
6th October 2013, 03:41 PM
Try swapping the ECU relay with the A/C relay under the bonnet.
If the ECU doesn't have power it can't log any problems or disruption in data readings.
Saying that, your problem sounds more...
6th October 2013, 03:36 PM
X 2 on the ECU relay one less thing to go wrong,
2nd October 2013, 09:22 AM
I had the same problem and mine turned out to be the ecu relay
1st October 2013, 08:35 PM
I still think that it's the pump regardless what mr nissan have said. My old mans did the same.
1st October 2013, 03:15 PM
has vehicle got nads? as roofy said it might be going into limp from over boosting.
30th September 2013, 09:26 PM
Sensor in the pump.
They put a reconditioned pump in. New lift pump. Crank angle sensor. $4770 all up
30th September 2013, 09:19 PM
Could be to much boost and going into limp mode
30th September 2013, 09:14 PM
Went through exact thing. Injector pump