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9th May 2016, 10:10 AM
#21
Originally Posted by
Touses
Hi bloke. How did you go with this?
The two stroke seemed to help. I can give it a little more before the black smoke comes pouring out, but still need to be sure not to drop the pedal to the floor- or anywhere near it for that matter.
Theres no Altitude Compensation System (Thankfully,) I'm at 5000 feet and this thing came from sea level so thinking about backing off the fuel a quarter turn. Though, also considering just taking it to a diesel shop.
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9th May 2016 10:10 AM
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9th May 2016, 10:22 AM
#22
Patrol Freak
Yeah good call on the fuel pump, it could well be over fuelling! Dyno tune would probably sort it out.
Did you notice a reduction in engine noise with the 2 stroke oil?
I AM NOT STUBBORN.........I prefer the term, Singlemindedly independent !
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9th May 2016, 10:50 AM
#23
Yup, definitely runs smoother with the addition of the 2 stroke. Though, could also be from burning off old fuel, not sure what was in the tank when I got it.
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14th July 2016, 06:33 AM
#24
Just heard back from the diesel tuner. Telling me it needs a light load advance adjustment, looking at a few hours of labor to pull the pump and get it on the test bench. Not a cheap ordeal.
Smooth idle, smooth start, starts sooting at 1/4 acceleration. Almost no soot in 1st gear, if you keep it redlined and shift into 2nd it just starts belching.
Anyone out there been through this? Does it make sense with the symptoms to you?
Last edited by sangersanger; 14th July 2016 at 06:47 AM.
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22nd July 2016, 07:40 AM
#25
Finally got it sorted. The pump was delivering 72 cc's of fuel, when it should have been down around the 50's. When they had the pump out they were a little dumbfounded as the tamper cap had never been removed. A few laps on the dyno and it's running great!
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22nd July 2016, 08:12 AM
#26
Patrol Freak
Originally Posted by
sangersanger
Finally got it sorted. The pump was delivering 72 cc's of fuel, when it should have been down around the 50's. When they had the pump out they were a little dumbfounded as the tamper cap had never been removed. A few laps on the dyno and it's running great!
So it was over fuelling. Good to see it sorted brother, big heaps enjoyment now eh?
I AM NOT STUBBORN.........I prefer the term, Singlemindedly independent !
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